.... preparatory to dropping in the engine, the clutch and transmission had to be bolted up. This presented its own set of issues. Biggest one is that the flywheel sits closer to the block. This moves the pressure plate forward and adversely changes the angle on the clutch fork. For a while I was not sure what to do but a little research revealed that there are longer throwout bearings. I found one on e-bay from McLeod that fits and installed it. I also bought a spare I thought. Just went out to the garage to get the part # and discovered that they sent me a Ford throwout bearing!!!!! This is just freaking typical of why it has taken so long. Now I have to deal with that......
OK, I'm back - part # is 160322829131. McLeod actually called back almost immediately and is sending out a UPS call sheet for the wrong part. Basically what this longer throwout does is compensates for the difference between the face of the flywheel and the face of the bellhousing between the two motors. Had to bolt and unbolt both a few times to figure out what was right.
The other necessary task to get the motor where it belongs is engine mount adapters and another adapter from VetteWorks to mount the so-called "Z-Bar" which connects the clutch pedal pushrod to the clutch/pressure plate pushrod. Made some changes there too. A quick look
A pair of heim joints and an adjustable rod should make this a step above the sloppy factory linkage. Note we no longer need the anti-rattle springs either.
Here is the motor in place
Everything is in place and more or less fits. The headers clear the new Borgeson box with over 1/2" of clearance. Legend has it that the Corvette oil pan doesn't fit the stock steering. But since the Borgeson let me eliminate the hydraulic RAM, it dropped in just fine. Also managed to get the stock alternator mounted which means the wiring for the charging system doesn't need to change.
The Vetteworks brackets worked as advertised in that I was able to bolt the transmission into the stock holes in the frame. I understand that the cylinder heads are further back in the block and they may be closer to the firewall. That will have to wait till I put the body on.
The differential felt like it was about to self-destruct when I pulled the car off the road and so I had Dave rebuild that as well. Turns out it was on its last runs, the ring gear bolts were scraping the case. I now have new Richmond 3:36 gears. Discovered while everything was laying around that I have an M20 wide ratio Muncie. Shouldn't hurt autocrossing at all and I will have a longer first gear. As I remember I was rev-limiting out at 6400 somewhere near 57 MPH. I expect the car will still smoke the tires anytime I want. Changing from the 3:55 that was in there will also give me a lower cruising RPM. Seemed like freeway driving was around 3800 or so, this will drop it down to something more tolerable..
And of course with everything lying around loose, it was a good time to get the driveshafts rebuilt with new Spicer universals. That's not cheap either. Here's a look at the backend.
This picture shows the VBP control arms, which have greased fittings. That was always a pain. I found a set at Mid-America that doesn't need fittings and installed them. Also discovered that the strut support bracket was cracked. Rather than weld it, got a new one. I'm sure there's lots more stress at that point with these solid strut rods and super sticky wide tires. The camber adjusting bolts have been replaced by the square plates with a only few adjustment settings. Cad plated in the picture. The inner placement of the bolts is up as high as I could get it to maximize camber change in turns.
It is a pleasure to be bolting up clean parts. It's difficult to bolt on something rusty now, generally everything gets derusted and painted.
Now for the things that really don't fit.
Z-Bar- Here is another view and what's different from stock is that the inner control arm had its weld Dremeled out and was then moved towards the block.
Trailing Arms - These are offset tubular arms from Global West. Thanks, I guess, Brett. They have a spherical joint where they mount to the frame and factory holes for the stock anti-sway bar. Everything went together normally until it came time to put in the emergency brake cable. Here's what I found.
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| The bolt is just a place holder to show where the emergency brake cable is supposed to go. It certainly won't go through this hole. |
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| Not very neat but at least the cable appears to fit. This is the wrong clip, it was just conveniently lying around. |
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| This S-Curve is quite a bit more severe than the stock route which trails under the arm and bends more gradually. I don't yet know how well this is going to works (or WTF they were thinking at GW) |
I had hoped to get some constructive feedback from at least CorvetteForum but that has not happened yet. Surely there is someone who's worked through this??
Accessories - Here's a good look at the front of the motor.
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| One serpentine belt takes care of everything. I got the belt length correct on the first try |
The waterpump inlet is aimed at the upper right control arm. No room for a hose. And the heater core inlet and outlet plumbing is too close to the control arm. With a little engine torque, they're going to hit. The former has been fixed with an inlet that comes straight in. To fix the latter I am going to have to remove the pump, thread the holes to NPT (they appear to be the right size, 3/4" and 5/8"), and install 45 degree fittings. Waiting for a package to arrive from Summit. Other people have done this so I am hopeful. These pumps are quite expensive! Look again at the front of the motor! This will have to wait for a future post.
Temperature Gauge - Last subject is the temperature gauge. Knowing that my stock gauge is going to be wrong, I sent out my instrument cluster and the "sending unit" to Red Line Gauge. John there sent me back my original sending unit and a new one matched to the movement he installed in the cluster. And a bunch of brass fittings, none of which fit my motor. About $90 for that so no big expense but one more problem not quite right. The GM unit is a two-wire sensor but it is basically the same as the one wire original in that it is simply a temperature sensitive resistance, and the second wire is a better ground than through the engine and chassis. Time to measure and plot some data.
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| Multi-meter set to measure resistance and has a handy thermocouple, plus a hot water supply |
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| I guessed that this would be a semi-log function. X-axis is temperature and the Y-axis is resistance. |
The bottom blue and red plots are the GM and aftermarket senders. The curves are not close enough. While I could match the aftermarket with a parallel resistance at (say) 200 degrees, everything else would be way wrong (the curved line). And since the GM sensor has higher resistance I would need to add a negative varying resistance in series to match the aftermarket. Not feasible at all. I despaired for a while and then voila inspiration. There's a hole in each cylinder head for these senders. If I put two senders in parallel, the result was pretty close and below the aftermarket. See top curve. A small (47 ohm) resistor in series with the two senders wired in parallel works great across the temperature range (ignore the 200 ohm comment in the graph)
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| Success |
good place to end the story for now




















